So I did some work on the 390 over the 4th of July- big thanks to the Husaberg tribe and elders for posting all their experiences. Very helpful!
Here are some notes:
At 50 hours the spark plug had some mild corrosion forming. I will be spraying some air in there after water exposure.
The tank wasn't too bad to remove, but the air box design makes it more work than other bikes. I added reflective fiber tape to the bottom of the tank and wrapped the fuel lines.
I did not like how the wire bundle running next to the TPS blocks the rotation of the plug and adjustment, so I moved the bundle more towards the inside of the frame and TPS adjustment is better now. I played with the TPS a little but still need more experimentation. Will probably set to 0.601V and be done with it. Not sure how the idle screw works yet. Does it open an air bypass or does it adjust the butterfly?
Some connectors had dirt starting to enter the pins so I cleaned with alcohol and added dielectric grease.
I checked the valves and the exhaust were fine on the loose side. The intake had one a little tight and one loose, so I swapped some disks and got them close to each other more on the loose side of the spec. I don't use a feeler gauge much, so I hope I got it right. I had to kind-of saw the gauge or push it in pretty good at max spec and over, so I think it was ok. Same for the intakes. I should have recorded the engine sound before the work for comparison. I can hear the valve-train - hope that is normal. It's not loud, but you can hear it. Let me know if it sounds concerning. It for sure doesn't sound like the tensioner failures I have heard in vids. I had to take the ignition cover off to get to TDC due to the old ball actuated Rekluse (Z-start pro), then used the TDC bolt by removing the copper washer from the bolt on the clutch cover. Probably overkill because at TDC there is a couple degrees of free cam rotation for things to go boom.
I added the ZipTy fuel filter- seems pretty good and the way it integrates with the quick disconnect is worth the money. I took out the grey little inline filter in the ZipTy. My bike had the small inline filter at the elbow connection to the throttle body removed, already.
I added the dirt tricks tensioner. Pretty easy install when you lay the bike over. Otherwise, the piston keeps falling to full extension and you can't tighten the cap down. Well, you can, but it will damage stuff. Be careful of that.
The Sicass key-switch is pretty nice. I like the action of it. Easy to install, too.
The Hyde Racing Bash plate is pretty sweet.
The Profill fast fill filter sock is cool. Fills fast. : )
Changed the oil, filter, and cleaned the screens. The engine was very clean inside. The guy I bought it from only used Motorex and K&N filters. Seems to do the job, but it only has 50 hrs on it. Couldn't find the Motorex over the holiday, so used 20W50 Valvoline motorcycle oil. There seems to be more drag on the Rekluse at idle now. I will experiment and use Motorex next oil change.
I performed the weep hole mod. It was much easier to take the clutch side off to take the water pump shaft out vs. dicking around with prying the seal out. The seal was of course installed backwards from the factory like everyone says. I planned on reusing the seal, if possible, so taking the clutch side off is the way to go. If you are going to toss the seals, just drilling a couple small holes in the seals and using a drywall screw seems like it would work. If it gives you trouble you might just want to take the clutch side off with the bike on its side, or combine with an oil change. There was fine dirt between the two seals, also just like everyone says. I cleaned it all out and sanded the shaft with 600 grit a bit, then reinstalled the seals. It seemed to be leaking a bit at some point because there was calcium or whatever in the seal bore. Just a little bit. The seals have a little groove in the middle of the bore, so I put some grease in there and lightly greased the shaft. The weep hole was gummed up, so cleared that out. Next, the brass tube I bought was sanded down on the tip and I tapped it into the weep hole (just the tip), then slipped on some silicone tubing down to the bash plate where I loosely zip tied it. Dirt be gone!
I installed the dirt trix engine sprocket spring washer - took the sprocket off and greased the splines. Also put grease under the spring washer and extruded grease through the spines as I tightened the bolt exactly to spec. Pretty sure that torque spec is pretty critical no matter which spring washer is used. The blue spring washer looks pretty snazzy.
The bike will live at 7000 feet so riveted the factory fan on the radiator. Checked the coil connections while I was around there. I flushed out the old coolant with water, then two pours of Evens prep fluid, then two pours of Evans no boil coolant. I like how the little drain screw port on the water pump doesn't drain until the radiator cap is opened. It seems to be a low point, so I think most fluid drains out. One 64oz bottle is about two system fills, so I should have close to the required 97% concentration. Maybe I should have thrown some compressed air in the system but I got lazy. Should be fine.
The rear silencer joint leaks, so going to throw some RTV on that at some point. Maybe the front joint, too. The new springs come soon and I will refresh the fork oil, bushings, and seals when I do that. Not sure about the valves and shims. Maybe the next time.
That's all for now!
Here are some notes:
At 50 hours the spark plug had some mild corrosion forming. I will be spraying some air in there after water exposure.
The tank wasn't too bad to remove, but the air box design makes it more work than other bikes. I added reflective fiber tape to the bottom of the tank and wrapped the fuel lines.
I did not like how the wire bundle running next to the TPS blocks the rotation of the plug and adjustment, so I moved the bundle more towards the inside of the frame and TPS adjustment is better now. I played with the TPS a little but still need more experimentation. Will probably set to 0.601V and be done with it. Not sure how the idle screw works yet. Does it open an air bypass or does it adjust the butterfly?
Some connectors had dirt starting to enter the pins so I cleaned with alcohol and added dielectric grease.
I checked the valves and the exhaust were fine on the loose side. The intake had one a little tight and one loose, so I swapped some disks and got them close to each other more on the loose side of the spec. I don't use a feeler gauge much, so I hope I got it right. I had to kind-of saw the gauge or push it in pretty good at max spec and over, so I think it was ok. Same for the intakes. I should have recorded the engine sound before the work for comparison. I can hear the valve-train - hope that is normal. It's not loud, but you can hear it. Let me know if it sounds concerning. It for sure doesn't sound like the tensioner failures I have heard in vids. I had to take the ignition cover off to get to TDC due to the old ball actuated Rekluse (Z-start pro), then used the TDC bolt by removing the copper washer from the bolt on the clutch cover. Probably overkill because at TDC there is a couple degrees of free cam rotation for things to go boom.
I added the ZipTy fuel filter- seems pretty good and the way it integrates with the quick disconnect is worth the money. I took out the grey little inline filter in the ZipTy. My bike had the small inline filter at the elbow connection to the throttle body removed, already.
I added the dirt tricks tensioner. Pretty easy install when you lay the bike over. Otherwise, the piston keeps falling to full extension and you can't tighten the cap down. Well, you can, but it will damage stuff. Be careful of that.
The Sicass key-switch is pretty nice. I like the action of it. Easy to install, too.
The Hyde Racing Bash plate is pretty sweet.
The Profill fast fill filter sock is cool. Fills fast. : )
Changed the oil, filter, and cleaned the screens. The engine was very clean inside. The guy I bought it from only used Motorex and K&N filters. Seems to do the job, but it only has 50 hrs on it. Couldn't find the Motorex over the holiday, so used 20W50 Valvoline motorcycle oil. There seems to be more drag on the Rekluse at idle now. I will experiment and use Motorex next oil change.
I performed the weep hole mod. It was much easier to take the clutch side off to take the water pump shaft out vs. dicking around with prying the seal out. The seal was of course installed backwards from the factory like everyone says. I planned on reusing the seal, if possible, so taking the clutch side off is the way to go. If you are going to toss the seals, just drilling a couple small holes in the seals and using a drywall screw seems like it would work. If it gives you trouble you might just want to take the clutch side off with the bike on its side, or combine with an oil change. There was fine dirt between the two seals, also just like everyone says. I cleaned it all out and sanded the shaft with 600 grit a bit, then reinstalled the seals. It seemed to be leaking a bit at some point because there was calcium or whatever in the seal bore. Just a little bit. The seals have a little groove in the middle of the bore, so I put some grease in there and lightly greased the shaft. The weep hole was gummed up, so cleared that out. Next, the brass tube I bought was sanded down on the tip and I tapped it into the weep hole (just the tip), then slipped on some silicone tubing down to the bash plate where I loosely zip tied it. Dirt be gone!
I installed the dirt trix engine sprocket spring washer - took the sprocket off and greased the splines. Also put grease under the spring washer and extruded grease through the spines as I tightened the bolt exactly to spec. Pretty sure that torque spec is pretty critical no matter which spring washer is used. The blue spring washer looks pretty snazzy.
The bike will live at 7000 feet so riveted the factory fan on the radiator. Checked the coil connections while I was around there. I flushed out the old coolant with water, then two pours of Evens prep fluid, then two pours of Evans no boil coolant. I like how the little drain screw port on the water pump doesn't drain until the radiator cap is opened. It seems to be a low point, so I think most fluid drains out. One 64oz bottle is about two system fills, so I should have close to the required 97% concentration. Maybe I should have thrown some compressed air in the system but I got lazy. Should be fine.
The rear silencer joint leaks, so going to throw some RTV on that at some point. Maybe the front joint, too. The new springs come soon and I will refresh the fork oil, bushings, and seals when I do that. Not sure about the valves and shims. Maybe the next time.
That's all for now!
Last edited: